QUIK CHOW

team 23 

team . mission . table . strategy . design . competition . journal . pictures!

This is the journal I took as secretary of the group. Click on a day to see the entry for that day. --Roxanne
sunday
monday
tuesday
wednesday
thursday
friday
saturday

2

3

4

8

10

14

19

21

28

30

 

wednesday, january 5, 2000

 

Monday was parts sorting. Justin hadn't flown in yet so Neil and I had to do an half an hour each. Yesterday was the first day of lecture. The staff introduced themselves and talked about the class in general. They presented the competition theme, and at the end, we got our kit of legos and stuff. Again, Justin still was not here and so missed the first lecture.

Before lecture today, I met with them both (Justin had come back) in their dorm. Neil and I opened up all the little packages we recieved in lecture yesterday. We looked at all the pieces, wondered what they did, and then sorted them all into tupperware and boxes. Meanwhile Justin read over the notes, contest rules, and whatnot that he missed because he was on a plane. We discussed a little bit of strategy, but nothing substantial or within reason (i.e. no teleportation was not an option).

In lecture, we learned some basics about sensors and actuators.

After lecture, we went back to the dorm and discussed more strategy. Should we try to put all the blocks in jail? Should we go for the professors? It seems we should definitely go for the two hackers on the side.

 

thursday, january 6, 2000

 

Today was the first day of recitation. We have Andy as our instructor, and Bernard (who was a no-show) for our T.A. In class, we discussed some potential strategies. This is when our team realized we read the table setup wrong, and that putting all the blocks on our side was a net gain of zero. Silly us. The last thing we did in lecture was to build a gear box. But our team didn't realize that we needed the kit for recitation so we just looked at the cool example robots that Andy brought to recitaiton.

After recitation we went and looked at the contest table. It was much bigger than I expected. With a better idea of that task at hand, we went back to the dorm to scheme and strategize and play with Legos. We decided it would be useful to attempt to built a gear box. And our attempt proved successful. We also discussed a couple of new strategies since the old one didn't make any sense.

 

friday, january 7, 2000

 

Today in the Java lecture, Neil handed me a paper listing two possible strategies. It was pretty detailed with a pros and cons list. Of course, Justin didn't make it to the Java lecture until it was pretty much over. I don't think he's a morning person.

Justin and Neil walked into the third lecture with a new strategy. We would go for the blocks that we were certain of, i.e. the two hackers beside the jail and the four professors. Today's lecture was about the controller boards. All three of us must have been pretty tired since we each fell asleep for about five minutes at one time or another.

 

sunday, january 9, 2000

 

We made a LOT of progress today. We began to piece together a semi-functioning structure based on our strategy. There isn't a lot, but it's a start. So far we have a four wheels with a motor box and gear train attached to each of the back wheels. For convinience, we didn't line up the front wheels with the back, a minor thing. If it's a problem, we can fix it later. Between the right wheels and the left wheels will be a channel so we can run over the blocks, going backwards and forwards.

My fingers are numb from pushing pieces together and pulling them apart. Why are Legos so sharp if they're made for kids?

 

tuesday, january 11, 2000

 

After recitation, we did some minor stuff in the lab. We wired together a couple of motors and conceptualize the door and channel.

 

wednesday, january 12, 2000

 

We realized that our gear ratio was really high because we used gears to connect the gear box to the motors. So we started over and redesigned the entire thing. We also attemped to make doors to keep the blocks in our channell. Neil and I accidently fell asleep while Justin continued to redesign. It was not the most productive day.

 

thursday, january 13, 2000

 

After recitation, we went to lab.  There wasn't much to do without a controller board so we did some easy stuff. More wiring together sensors and motors that we had, bracing, and redesigning the shape. We're working on how to attach the wheel to the door on a servo.

 

saturday, january 15, 2000

 

   Justin has gone to NYC, so Neil and I went to lab to feel productive.  We figured out what sensors we would need to implement our strategy/design.  About four of our points were used up buying extra sensors, and ten dollars was used to buy another servo.  We stayed for about four hours wiring up our sensors, the new servo and the second battery pack.  We also used some cardboard to make a preliminary cardboard channel.  We will try testing this channel out before making the real one out of the base plate.

 

sunday, january 16, 2000

 

Now both Neil and Justin are gone.  Justin is still in NY, and Neil went skiing.  I stayed behind and worked a bit on the code, but its hard without the controller boards..

 

monday, january 17, 2000

 

Hmm... still, no controller boards.... strange. Today, we worked on coding so that by the time we got the boards, we would be ready to test.

 

tuesday, january 18, 2000

 

 Today right before recitation we got our controller boards. In recitation, the organizers showed us how to upload the kernals and our code.

After recitation officially ended they ripped the boards away from us. Reason: the boards had a tendency to blow up. Fun fun fun!

The team headed home to work on the bot and the code. We were able to get the front door with the servo working well. It should hold because it was braced better. Most of the code is relatively unchanged. We have about 3 or 4 days until the mock competition. I think the team is less than eager for Judgement Day. The robot should at least move forward. Hopefully.

 

friday, january 20, 2000

 

I think I caught a cold or the flu.  Going snowboarding last night didn't help.  I stayed at home and tried to code, though I wasn't very efficient in my flu state. 

Meanwhile Justin and Neil went to lab for most of the day.  They stayed from 11 A.M. to 8 P.M.  They tell me it moved for the very first time.  I'm sad that I missed our baby's first steps... er... well, technically it rolled. They worked on the code mostly (Neil's laptop proved to be very useful).  They calibrated turns in code by random testing.  The "DifferentialDrive" code provided for us was removed, because our robot was not driving straight.  Instead, it would zig-zag in a diagonal across the board.  So Neil wrote a new differential drive routine.  This new routine did not use shaft encoding to drive straight, instead the stronger motor is driven at a harded-coded percentage of the other.  They also built a place for the skiffboard and battery pack.

 

saturday, january 22, 2000

 

Today we met at 11:30 in the lab.  Before we went to lunch, everything was working swell.  Justin and I planned out the form and shape of our channel, while Neil wired more sensors.  Since Justin drove to lab (because of the large amount of stuff to haul), we decide to treat ourselves to a nice lunch at CPK.

After we got back to lab, we managed to successfully destroy *THREE* skiff boards.  The first mysteriously stopped sourcing power to the motherboard.  The second as well the third started smoking after the code was loaded. 

We decided to hold off on trying anything with the new board.  Justin and I made the channel from the base plate and Neil looked at Interactive C.  While Justin was having fun bracing our new channel (as bracing is his favorite hobby), Neil bitched at the computer, very annoyed at having to switch to the far inferior language of Interactive C. 

Neil became sadistic.  "I want to burn a board.  I want to burn a board."  I think the task of porting our code from Java to C, squished all the hope out of his poor little soul.  He turned into a bitter, pesimistic man.  Poor Neil.  Justin and I agreed that Neil had completely lost it.  He was talking and cursing to himself.

Our fourth skiffboard seemed to be working fine.  Our bot consistently grabbed to two hackers and deposited them into our jail.  GO ROBOT! GO!!!  It seems to move up the ramp, but turns more than 90 degrees.  Going for the hackers on the the pyramid is not reliable yet.

 

sunday, january 23, 2000

 

I have brought my laptop to lab so that I can type the journal as the days go by. My memory at the end of a long day is crappy . Plus, I forgot to enter in a couple of days worth of entries for the middle of this week.

Tomorrow is the mock competition.  We hope to have a completely functional robot by the end of today. Unfortunately, one of the gears on our motors came off last night. As a result, we began the day by repairing this motor, as well as finishing placement of our last few sensors. Fixing the motor somewhat upset our previous calibrations. After we fixed the motor, we tested out our beacon and our orientaiton routine.  Since it always thought it was facing right we debugged the routine.  It took a while to fix it completely debug the code.

At the same time, we modified the channel to make it extend further outward.  This made room for the front two push button sensors.

We're going to code line following or line detection. "ahhh fawck!"

7:10 : We're going to go to eat now.  

We ate at MacDonalds. 

I don't like lego.  I don't like sensors or actuators.

Neil has A LOT of errors in his code. So we must wait.  I have no fucking clue how this robot is going to win anything.  Neil is talking to himself again.  Tension is rising.

EVIL MEAN people keep taking our tools without asking!!!!  I have taken measures to ensure that they will pay a very painful price.  Most of the tools are sharp enough.  How ironic that the tools they steal to help them can also hurt.  I await for blood.  Vengence shall be mine!!! MUHAAAAAAAA!!! 

roxanne is now off her rocker -Neil

Technically it's monday now...12:30 A.M. The robot drives pretty straight! Woohoo! Justin wrote some code to make the robot figure out when it's on the yellow line using our new LED/transistor pair, but as of yet, the robot remains confused. Apparently, the processor can't handle reading the sensor and running the robot at the same time, so it tends to overshoot the lines =( how sad. Stupid board.

This is my one entry in the journal. -justin.

4:25: We give up for today/tonight.  We're all tired.  Neil says he's not being productive. So we're going to stop for tonight.  I offered to stay on working if Justin wanted to but he decided that we should go home.  I don't mind.  Someone is playing mediocre music and then singing way off key to it.  They both think I need to sleep some because I'm still a little sick.  Maybe they're right.

So far the new differential drive works somewhat well. In addition, the light sensor that we placed on the left side of the robot allows us to get onto the ramp accurately on the longer axis of the board. Unfortunately, our turns aren't quite as accurate.. perhaps because of voltage problems or just plain inaccuracy. We need to work on that if we want to continue with our current strategy. In any case, we'll try to do this so that we can grab one of the profs, hopefully, and then continue with the rest of our strategy, since orientation isn't too hard with the walls around us and the light sensor. 

Tomorrow(today), we'll need to practice calibration, make sure the go sensor works and turns off after 60 seconds, and then we should be ready for the mock contest. After seeing how much work went into getting the first part of our routine down pretty well, I would hope that since the other teams, for the most part, are behind us, that we will kick their skinny little asses all over the freaking board tomorrow if they dare go up against us. we're the only team that's been here pretty much continuously since 11 am yesterday morning. Justin says the robot is falling apart. i don't care. let it die. die die die. 

That last message was brought to you by Neil. I think he wants to go to sleep.

Unfortunately for Neil, Justin keeps saying "Just one more run". So Neil chokes himself to death with his scarf. Finally after 30 minutes of "one more run"s, we're going home.

 

monday, january 24, 2000

 

We woke up early today.  Because of techinical difficulties the full team wasn't together until 11:15 (i.e. I was late).  We played with the 90 degree turning and saw that the bot would turn different angles at different points on the table.  Next we worked on the calibration and orient routine.  Today's the mock contest. I think we'll enter.

WE TOOK THIRD PLACE!!! YAY!!!  Well, so it was only out of 7 teams but we did well all things considered .  At least we had the confidence and the robot to enter.  That's more than a lot of teams can say.

Arg!!! I want to give up.  It doesn't seem worth the time.

Now we're trying line following.

This is my second entry into the journal. -justin.

Okay, they went to eat.  I'm sitting here feeling sorry for our robot.  And how pitiful it is.  It started out as a really cool robot.  Everyone was impressed by its speed and turning ability.  But now... well, it doesn't seem so impressive.

Our biggest problems are going straight.

Our turning ability was improved by magnitudes after we started using the sum of the right and left encoders, which appears to compensate for the different turning ratios that are required by the slope of the table. To do this, Roxanne coded something that would allow us to hold a button down until the turns were calibrated. woohoo.

Now, we're go mostly straight, so the robot is now good to go.

ow my head hurts;
void killRobot() {
  useHacksaw();
 useHeatGun();
  useBigHammer();

if (!RobotDeadYet){
  ScreamInAnnoyance();
  throwRobotAtAnnoyingRobotWithArms();
}
}

-Neil 

I am a stupid moron. I need to pee. I going insane. blaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaaah!!! I want to sleep.

Justin staying
Neil and I home going

we come back 8 morning.

 

tuesday, january 25, 2000

 

Oops. I just erase the journal entry so far for today. I'll try to recreate the jist of it....

Today is Round 1.  We're trying desperately to get our act together.  I think we have a good shot given that many other teams are only trying to qualify. 

We don't have everything perfect, but hopefully it will do something right.

We're practicing the robot with all the code even the calibration routine.

This is my third entry into the journal. -justin.

YAYAYYAYAYA! we won our first match.  I think we got very lucky.

 

wednesday, january 26, 2000

 

Today is much more relaxed atmosphere than the past couple of days. We've won the first round which is much more than we had expected.It seems we were VERY lucky too, because the direction we faced happened to be the best one for our robot.  It's a good little robot.  We love our robot.

We're trying to make our robot a little more dependable in all situations. After it gets the first two hackers, it isn't reliable.

Neil has found a LED panel.  It looks like the one for the start light. He taped it to our bot.  I think he's trying to disorient the other bot. In the end, it will be removed because it's blinding me.

We added a lot of anti-stall and anti-getting-cornered-in code so that our robot will (hopefully) be able to maneuver itself if it gets caught somewher eon the board, either through its own inaccuracy or through the actions/position of the other robot. We're also doing some testing on how to run over arms. 

Our turns are really good, but only if the voltage is above 6.1 V. We borrowed a multimeter from Mr. Yip so that we can check our batteries during competition and make sure that this conidition is satisfied.

It's pretty crazy in lab now. Only three hours to impoundment, but there seem to be quite a few teams that haven't qualified yet. How scary.

OOOOOH a PERFECT RUN!
Hopefully we go against a placebo.

This is my fourth entry into this journal.  -justin

ARGH! our orienting method stopped working! Apparently, our sensor is too close to the edge of the light box, so that it ends up not detecting the light. However, with three hours until the new extended impounding time, we were able to write a more robust orientation code than the 'find brightest light' code we had been using. Just glad we caught it before impounding.

After we did orientation, we tested a couple more times.  Lab is packed.  And we keep wasting our table time because it rarely works all the way through.  The pressure is on.   Hopefully competition will be better.  Like its designers, our bot works under pressure. 

 

thursday, january 27, 2000

 

The competition was exciting.  Our bot placed somewhere between 6th and 9th.  More than we could have hoped for when started this journey in the beginning of January.   It was upsetting that the "Quik Chow" decided to stop functioning after facing "King Louie" in the third round.  We think their was some mechanical error that we couldn't see.  It was performing well on the table in lab.  Something happened between impounding and competition, which made it hop over the blocks and get caught in our channel.  It was a little disappointing that our robot failed to do what it was designed to do in those last few rounds and that it made it that far only on luck.

It seemed that a lot of the top teams only had luck on their side and it was not because of unique design or robust coding.  We were very impressed with the teams that actually sorted, such as Team 54 ("Handy Job") and Team 32.  Even though they didn't work perfectly they had great potential given more time.

Seeing it perform out there along with the others, there were one possible design  changes that came to mind.  The channel could have been made a little wider and lower to the ground.  This would have prevented hopping over the blocks. We were limited by the lab space and the amount of time. If there had been more tables to practive on maybe we would have a better robot. But we gave it our best shot and that's what counts. It was fun and exciting and learned a lot because of the cool staff.